ADDITIONAL RUNNING DAY - 31st July 2010 47401 has been requested for a further short notice vice-steam turn, this coming Saturday, 31st July. It is rostered on the MR-B's Timetable "A", thus will be working four round trips beginning with the 1115 ex-Butterley.
FLEET UPDATE - 1st July 2010 47401 (D1500) The fleet pioneer successfully completed its booked workings on Sunday 20th June, clawing back some of the mileage lost earlier in the year after the fan motor failure. The loco was (briefly) out again the following weekend on Saturday 26th June. Class 14 No. 14901 failed at Swanwick during the MRB's shunter event and although initially a Swanwick-Riddings-Butterley passenger run looked on the cards for 401 in its "Thunderbird" mode, to the disapointment of several passengers the train was cancelled and 401 worked ECS Swanwick-Hammersmith-Butterley then light engine dragging the "Teddy Bear" back to Swanwick. Some photos of the rescue job appear on the 47401 Gallery Page.
D1516 (47417)
The air tanks are being refitted to the locomotive as and when
space allows. Like many things, the air tanks need other elements of
the locomotive to be complete prior to installation. For instance the
auxiliary room conduits, which are inaccessible with the "torpedo"
tanks in situ need checking for cable condition and conduit condition.
More auxilliary machines have been reunited with the locomotive,
including the traction motor blower at No. 2 end, which looks excellent
amidst the sea of grey and white paint which has transformed the
appearance of the area. A lot of hard work has been put into cleaning
this area of assorted corrosion and general detritus, and it's a credit
to the lads who undertook it.
The cooler group has now been thoroughly cleared of
corrosion, cleaned and painted. This will then be moved to a secure
location prior to fitment of its elements and subsequent hydraulic
test.
The locomotive body is having weld repairs undertaken by the
Midland Railway Trust's staff, to put the body side steps back to
rights and replace a corroded section of the body at No. 2 end (the
same area we replaced on 401 some years ago).
The severed cables in the auxilliary room are gradually being
replaced. The conduit which runs the length of the of the auxilliary
room has had the cables removed from it for inspection. These have
been suspended at several points along the bodyside, allowing the
corroded length of the conduit to be replaced. Photos of recent work can be seen in the 47417 Gallery.
47761 (D1619 - 47038 - 47564)
The body of spares donor loco 47761 has been sold by the Project to Harry Needle Railroad Company (HNRC) in a cash plus spares deal, having already contributed much useful equipment towards the restoration of 47417. A bogie swap will be undertaken before the faded RES liveried loco departs for pastures new, 47761's bogies being destined for 47417.
47401 20th June Extra Trip
401 will now be working six round trips in total this Sunday (see news item below). An extra 16:20 ex-Butterley departure has been added as compensation for the reduction in the advertised service from "Timetable C" to "Timetable B".
Also, some new photos have been added to the 47401 and 47417 Gallery pages.
47401 UPDATE - 16th June 2010
47401 will be running this Sunday 20th June, vice steam loco, working five round trips starting from Butterley at 10:20. Note the MR-B website advertises this day as "Timetable C" (two train running) but it has been reduced to "Timetable B". Timings are here.
The loco performed well at the Diesel Gala (see below) though the last trip on the Sunday was knocked on the head due to running low on fuel.
47401's next working following the gala was a Driver Experience day on Friday 11th June, and again the loco performed well on a series of light engine and stock moves, the customer who had chartered it seemingly very happy to have a 47 for his big day. Anyone interested in doing the same should contact the MR-B direct.
47401 UPDATE - 19th May 2010
47401 is back to
operational status as of last night. The failed fan motor went off site for repairs but
duly failed when bench tested following initial remedial work. Further
work has been carried out and this delayed its return. However we are pleased
to report that the motor is now back and over the past two weekends we
have reunited it with its cowlings and the whole assembly is now back
inside the loco. On Monday evening 17th May the loco was run up
to double check all the other 800v machines were OK and then last
night it was the same again plus the fans. So subject to the usual caveats 401 will be
performing at the MRB diesel gala this weekend. A word of caution for
the purists, it's a top and tail affair with several visiting locos. I
believe we have 45133 for company on a couple of turns and then the
visiting Class 14.
So our thanks to Richard Ward, Paul Parker, Tom Gray, John Ward, Martyn Catlin, Ian Crampton
(plus his ‘Assistant’ crane driver) for their efforts
over the last few days.
Here is the link to the full info on the MRB diesel event with details of the three visiting locos.
D1516 UPDATE - 22nd March 2010
Monday 22nd March was another milestone day for D1516. The
event taking place was the hydraulic pressure testing of the locomotive’s air
tanks. Some of you may recall that these tanks (47401-20 each have 17 air
tanks) were removed from the loco almost two years ago and an initial inspection
resulted in four of the tanks being failed. Owing to the unique nature of these
items it has taken a long time to source replacements which eventually resulted
in three brand new tanks being constructed and one tank being reconstructed. In the
case of the latter the inspector deemed the shell of the tank was defective but
the dished ends were okay.
Having obtained our replacements we have held back from the
second phase of testing until we were close to completing the refurbishment of
the auxiliary room and its roof section which is where most of the tanks are
situated. This also includes the overhaul of the various auxiliary machines
that occupy this compartment as some of the air tanks are positioned under
these machines. So with the end of these tasks in sight it was time to carry
out the pressure test.
We had 13 tanks to test, two of which are ‘dual’ chambered
giving us 15 tests to undertake in all. In addition it was also decided to test
one of the new tanks simply to bring its test date more into line with all the
others. So physically we had in one large tank to test A2 (the "torpedo" - for those of you familiar with 47s this sits under the compressors), three medium tanks to test and ten small tanks.
The testing itself is straightforward enough but time
consuming so in order to speed up the process some of the tanks can be coupled
together and tested as one. Generally the working air pressure system on a
Class 47 is 140psi which means for testing purposes you must test upto 1.5
times ie. 210psi. However to complicate matters a few of the tanks work at
different pressures to others so you have to be careful on ‘doubling up’. With
that in mind valuable brain power was expended putting together a running order
of tests taking into account the couplings available – male/female threads,
size ¾bsp, ½ bsp etc, etc. Quite simply
you then fill up each tank with water and the inspector pumps this up to the
required pressure and then makes sure this holds over the next 10 to 15
minutes.
Come the big day we got off to a flyer and by lunch time seven
tests had been completed, which included the dual chambered air tanks one each
of which sits under the driver’s seat – these are peculiar to the ‘Generators’.
Apart from a slight ‘weep’ from a reducer all went well and while this testing
was going on the ‘torpedo’ was moved onto a forklift truck and placed in position.
Our first minor hiccup came with tank A4 which I’d hoped to double up. Having
filled up its partner and connected the two up it was then realised that A4
contained not only a filter but also a further reducer meaning it would take
ages to fill up even though it was only a small tank. With its ‘mate’ ready
they were split off and A4 was eventually tested solo.
Just after lunch the threatened rains set in and we had to
move undercover. Rain is not very helpful when you are checking for potential
leaks. We had three small tanks left to do and then the bigger items, which to save
time we had already begun to fill up. Filling up an approximately 280 litre
vessel through a small ½ connection is not a quick job. However we soon arrived
at our nemesis A2 the ‘torpedo’. Pressure was applied but unfortunately at
about 100psi the blanking plates started to leak rather badly with little
fountains of water appearing. So whilst the blanking plates were taken off and
tried again the remaining medium sized tanks were tested.
After two further attempts with the ‘torpedo’ a combination of
PTFE Tape, Boss White and Horse Hair finally cured one leak and brought the
other under sufficient control to allow the test to be carried out at the
designated pressure and that was it, no leaks, success.
All we had to do now was pack up and empty out all the
water. By now the rain had stopped and the sun came out to shine on a
successful day. Our thanks to Martyn, John, Paul and Richard for giving up their time.
Over the next few weeks the air tanks will be repainted and
then put back in their rightful place. D1516 will internally start to look a
complete loco again.
47401 UPDATE - 1st March 2010 A bit of bad news we're afraid.
We are sorry to report that on Thursday 25th February 47401 had a flashover and has consequently has been taken out of service.
The loco was involved in a one day commercial testing contract hauling ECS.
Following several runs with a rake of stock the loco was idling when No. 1 fan motor flashed over. Quick action by the crew ensured that
damage was kept to a minimum.
For those who may be wondering it was a non-passenger carrying event,
not open to the public which is why it was not advertised. So rest
assured no chainage/mileage was lost! We do sometimes receive this type
of work which tends to generate more income for the MRB than for the
loco itself. On this occasion though it provided us with the
opportunity to use the loco and check for any faults prior to its
planned running days in March.
If there is any good news amongst this it is that only No. 1 fan motor was damaged and the 800 volt generator was unaffected. Whilst we
do our best to ensure the commutators and brush boxes are kept spotless
and the loco is tarpaulined during the worst of the winter it is suspected that a
combination of damp and possibly a build up of carbon in areas
inaccessible to us have contributed to the cause.
Anyway, Bowers Electrical Machines have already been on site to give
their professional diagnosis and the motor will be sent away for
repairs. The surmised reason for failure is that fixings
within the stator had exposed metal as a result of corrosion and resultant
degradation of the anti-tracking paint covering them. Normal Brush practice
would be to shroud said studs in winding tape, set with resin which would offer
superior insulation and prevent corrosion of the fixing undermining the
insulation so profoundly. The resultant flash-over has affected the
integrity of the cable insulation (local to the commutator) on the motor’s
stator which is to be replaced by Bowers. The commutator has also
suffered damage, which will be remedied by re-machining. The machine will
then be thoroughly cleaned and re-finished with anti-tracking paint.
The motor un-affected by the flashover had similarly unprotected
fixings. This is currently being remedied using tape, resin and anti-tracking
compounds whilst the machine remains in situ on the locomotive. Prior to
this the machine was thoroughly cleaned. Additional anti-tracking paint
will be applied onto exposed areas of the stator following a forced drying of
the rotor and stator. Hopefully this will reduce the probability of
further failures.
Some photos of the errant motor being lifted out are on our 47401 Gallery page.
Repairs to the flasshed over motor should occur in the next two to three weeks. Regrettably this
does mean that 47401 is not now going to be available for its running
days on March 13/14.
Apologies to those of you who may have had plans to visit but
hopefully the advance notice will allow you to change your
arrangements.
Assuming the loco is repaired in time then the next planned running day will be the MRB Diesel Gala 22nd/23rd May.
Not a good start to the new season, things have been progressing so well of late.
CLASS 47 DATA FILE PART 2 - 4th February 2010 Finally! The book is complete and is being delivered from the printers tomorrow. We have banked the cheques this afternoon of everyone who has paid via that method and hope to despatch all the back orders durover the course of next week. Meanwhile Part 6 is on the way (D1682-D1714)! To order Part 2 just click on the Book Sales page of this site (with
Paypal payment), or alternatively by cheque/PO payable to 47401 Project
(send to 21 The Oaklands, Droitwich, Worcestershire, WR9 8AD). Cost is
£9.99 + £2 P&P. WEBSITE EMAIL CONTACT - 5th January 2010 It has been brought to our attention that some emails sent to the Project via the contact link on this site have not been getting through to us. We have therefore replaced it with a direct email address - enquiries47401project@hotmail.com - you can either click on this link or cut and paste it into your address bar. If you have tried contacting us before and received no reply, sorry, we haven't been ignoring you! Please try again and we will get straight back to you.
CLASS 47 DATA FILE PART 2 - 5th January 2010 We are expecting this book back from the printers anytime now, it did not quite make it in time for the Christmas holiday period due to a few corrections and alterations being required to the completed page proofs. We will post a further update when we receive the book, at which time we will also bank the cheques of everyone who has ordered. If you haven't ordered yet then you can do so via the "Books" section of our for sale pages on this site (with Paypal payment), or alternatively by cheque/PO payable to 47401 Project (send to 21 The Oaklands, Droitwich, Worcestershire, WR9 8AD. Cost is £9.99 + £2 P&P.